Almost solved Intermitten Hesitation - take 2

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krisr
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Almost solved Intermitten Hesitation - take 2

Post by krisr »

Ok, please no crossposting as I really need ideas as to why i'm getting this RPM spike/dropout problem. This is the sort of problem that would make or break an ECU to the general person on the street so any help is much appreciated...

My combo:
400 Pontiac, 42lbs injectors, 78mm LS1 throttle body.
MSD Probillet distributor with VR sensor sent straight to MS2's VR circuit. IGBT driver firing an MSD6AL.
MS2 v3.0, 2.35 code. Fuel pressure set to 44psi at idle, with vacuum line attached it drops to 40psi.

Attached is a zipped datalog, the RPM spike is very noticable at about Record 15000 (see screen trap) and also attached is my MSQ if anyone can find something...

Thanks heaps!

Image
Last edited by krisr on Fri Apr 21, 2006 6:41 am, edited 2 times in total.
Sydney, Australia
Successfully MS2 v3.0 squirted 1971 Holden Monaro HQ
400 Pontiac, ported #16 heads, Tomahawk intake with custom plenum using LS1 78mm throttle body dialed in with a TechEdge 2E0 Wideband Controller.
krisr
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Posts: 137
Joined: Wed Aug 17, 2005 12:17 am
Location: Sydney, Australia

Post by krisr »

I replaced the VB921 driver, still no good. Dropped my dwell & spark duration from 25.5 to 2.8-3.5, didn't change. Added some heat insulation behind the MS box where I mounted it on the cabin side of the firewall, still no difference. I upped the fuel pressure to 50psi and reset REQFUEL/ve table, no joy there.

Without having access to a CRO to check the 'cleanliness' of my tach signal, would adjusting the VR pots make any difference? I also added a bit more RTV around the crystal on the mainboard just incase it came loose.

One other symptom I found when coming home just then, after a few violent hesitations, it just shut down. Switched ignition off and it fired right back up fine...

Any ideas, hints, tips?

http://www.reberger.com/Images/rpm_spike2.jpg
Sydney, Australia
Successfully MS2 v3.0 squirted 1971 Holden Monaro HQ
400 Pontiac, ported #16 heads, Tomahawk intake with custom plenum using LS1 78mm throttle body dialed in with a TechEdge 2E0 Wideband Controller.
Keithg
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Location: Chicago, IL, USA
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Post by Keithg »

I am also experiencing a similar issue with my 4cyl. Big rpm spikes. Thsi only showed up when I started driving a wasted spark setup. With a single coil deriven by a single vb921, it worked great. It has to be noise getting onto teh board either through a sensor, power or ground. I have not yet been able to track it down.

KeithG
krisr
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Joined: Wed Aug 17, 2005 12:17 am
Location: Sydney, Australia

Post by krisr »

What's your RPM signal? VR, hall, points...etc?

I'm going to buy a new pickup on Tuesday to try as a local speedshop has them on special at the moment, but beyond that, i'm a bit stumped. I replaced the VB921, put a pullup resistor on the output, but the dutycycle going to 0% on each stumble has me believing i'm definately having the problem on the RPM signal side of things...
Sydney, Australia
Successfully MS2 v3.0 squirted 1971 Holden Monaro HQ
400 Pontiac, ported #16 heads, Tomahawk intake with custom plenum using LS1 78mm throttle body dialed in with a TechEdge 2E0 Wideband Controller.
Keithg
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Posts: 45
Joined: Sun Mar 06, 2005 8:15 am
Location: Chicago, IL, USA
Contact:

Post by Keithg »

I am using wheel decoder (36-1) and a hall sensor through the optoisolator to sense the teeth. I am using MSnS-E 029o

KeithG
72_bay_simon
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Post by 72_bay_simon »

Sounds unlikely I know, but I hd all sorts of rpm spiking problems on my 4cyl VW install. I fitted a set of resistor type plugs and it was like a miracle cure! Runs and idles really smoth now. Worth a try for the sake of the price of a set of plugs!
krisr
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Posts: 137
Joined: Wed Aug 17, 2005 12:17 am
Location: Sydney, Australia

Post by krisr »

SOLVED!..

Thank you Dieselgeek! You've gotten me out of strife again!!!!

I have adjusted the hysteresis pot about 4-5 turns out until the RPM was a bit more smooth, then I even got a bit more creative and adjusted the zero crossing until it picked up RPM slightly, then back it off 1 turn.

Went for a drive, not 1 hesitation or stumble!!

Finaaaaaaally I can finish tuning this thing properly
Sydney, Australia
Successfully MS2 v3.0 squirted 1971 Holden Monaro HQ
400 Pontiac, ported #16 heads, Tomahawk intake with custom plenum using LS1 78mm throttle body dialed in with a TechEdge 2E0 Wideband Controller.
dieselgeek
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Posts: 19
Joined: Wed Sep 08, 2004 11:27 am
Location: Omaha, NE

Post by dieselgeek »

Good timing, we found ourselves in a similar situation this weekend and I was determined to try to figure this out.


ADjusting the pots for the specific VR installatoin seems to really do the trick, I've had a couple other guys comment on this as well.


Playing with the Hysterisis and zero crossing pots (is that what they're called) while having someone slowly spin the distributor until it triggered smoothly at low RPMs really helped us.


glad to hear you have it running,

-scott
Successfully Squirt'd: lots.
krisr
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Posts: 137
Joined: Wed Aug 17, 2005 12:17 am
Location: Sydney, Australia

Post by krisr »

Quick one.. Did you ever mess with the reluctor/pickup airgap in your probillet distributors? From memory I set mine to about 0.010" and MSD said it's a bit to close. They recommended about 0.030"...

That might contribute to my noise problem too?
Sydney, Australia
Successfully MS2 v3.0 squirted 1971 Holden Monaro HQ
400 Pontiac, ported #16 heads, Tomahawk intake with custom plenum using LS1 78mm throttle body dialed in with a TechEdge 2E0 Wideband Controller.
dieselgeek
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Posts: 19
Joined: Wed Sep 08, 2004 11:27 am
Location: Omaha, NE

Post by dieselgeek »

I'v enever played with the air gap settings on these distributors.


It would be interesting to see what happens when closing down that gap a bit, using an oscilloscope. My guess is that the A/C signal is higher amplitude? and might contribute to better low RPM performance, but maybe at the trade of high RPm tach spikes or problems?


-scott
Successfully Squirt'd: lots.
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